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Motor Rewinding

14814 Views 73 Replies 14 Participants Last post by  howmet tx
9
Armature rewinding
A beginner's guide

Every one at some time has looked for that bit of extra performance but how to get it, in the past it was easy as small firms and individuals often offered rewound motors and armature at affordable prices, sadly those days have gone and performance sometimes can be costly. However there are people out there with boxes of old motors craving to learn the lost black arts of motor winding, so for those out there as mad as I am, read on.
For the purpose of this article I will use an old Johnson 111, as this is a motor often in need of a boost and the technology here can also be applied to the scx and team slot can motors. S can Mabuchis are best left alone at this stage as the poor brush gear can lead to problems
Requirements.
Motor suitable for rewinding (in good condition, good bearing and brushes etc, worn out bearings and shafts will only lead to vibration and poor performance)
Wire to replace original, this is available from good electronics shops such as Maplin.
For this article I will be using 36 SWG enamelled copper wire.
Epoxy resin
Linen thread
Solder, and a soldering iron
A sharp knife
2 razor blades
A piece of modelling clay and a selection of small drills

Step 1
First thing we have to do is strip the motor to its component form very carefully making sure we don't loose ant of the springs or tiny washers .If you are using a Johnson motor carefully file off the serrations on the shaft to allow it to slide past the bearing with out damaging it. Check all the parts of the motor are in good order and the brushes and bearing are not worn.



Step 2
Carefully remove the old wire from the armature; this is best done by slicing through the old wire with a sharp knife.



When you have done this inspect the armature making sure none of the old wire is left on and the insulators at either end of the armature stack are in good condition, this is important as if there are any sharp edges the new wire can be damaged when winding. As you get more experienced you can trim these insulators slightly to give more room to pack the wire in but at first leave alone as it's just something else to go wrong.
Next we need to determine which way the motor is going to run by timing the commutator. On the standard motor the com is set with the slots in the centre of the web, by turning in the direction of rotation will determine which way the motor runs fastest (see diag). With a motor like this I would not use more than 10 degrees advance on the com as you may loose brakes and generate heat due to the poor quality magnets in these motors but, as we are just doing a simple wind, I don't propose to change the magnets at this stage.



Once you have determined the amount of advance, a spot of super glue will hold the com in place.

Step 3
Winding the armature.
For this motor I have chosen 120 turns of 36 swg with 5 degrees advance which will give us a fairly high revving motor some where in the region of 35 - 40K with a good spread of torque and reasonable brakes.
Clean the enamel off the end of the wire and solder on to the first tab making sure you have a good joint. Ordinary multi core solder is ok with a wind of this type, as it should not get too hot when running.



Now start winding onto the first pole in a clockwise direction, (some say you should wind in the same direction as you advance, at this level it doesn't matter to much, the motor will run fastest in the direction of advance, as I am right handed I wind clock wise). Try to get the wire to go on tight and even laying the wires on evenly in rows, stopping every 5-10 turns if necessary to pack them down with a match or a popsicle stick until you have reached the required amount, Take care not to over stretch the wire as it is easy to snap when using thin gauges such as these.



When you have completed the first pole loop the wire over the next comm. tab, clean the wire and solder before moving on the next pole.



Repeat the process and finish off by soldering the remaining wire onto the first tab.
You should now have a rewound armature, If you are just practicing winding on an old motor I would say just wrap a couple of layers of tape round the stack, put it in the can and stick 12 v through it to see how it runs. But if you are happy then continue to the next step

Step 4
Epoxying

Epoxying and tying is an important part of a rewind because it is unlikely that your wind will be as tight as a factory wind and there is the chance that centrifugal force will throw the wires off, so in order to prevent this we must stick the wire to the armature with epoxy resin also to prevent the com letting go at high revs we tie a bit of linen thread around it and epoxy that also.
There is a knack to getting an even coat of epoxy to the armature the trick is to get it to flow into the winding and penetrate not just sit on top to do this first warm the armature under a grill on a low heat setting for a few minutes, be careful not to burn your hands or use too much heat as to damage the arm, mix a little epoxy 5min araldite is ok for this and carefully apply to the hot arm, the araldite will thin and flow into the winding and around the thread which you have wrapped around the com ,take care not to get any on the com segments as it will insulate the electrical contact once set, just use enough to cover the wires don't build up a great covering you wont gain any thing and it will just make it harder to balance later, Stick the epoxied arm back under the grill for a couple of mins while it hardens then let it cool before handling .
At this stage we have a usable armature just in need of the comutator polishing, do this by putting it in a drill and touching the com with a hard eraser this will put a shine on it and help the brushes to seat properly, with poorly made /mass produced coms like these it is unlikely you would be able to true them up using a com truer, It is certainly impossible with the scx and Mabuchi s as these will disintegrate at the thought of it The Parma /mura and slot-it can be done with out a problem



Step 5.
The next step is to balance the armature in order to damp down some of the vibration
Commercially produced armatures such as mura, proslot, koford are dynamically balanced on a vibration analyser, we cant do this on the kitchen table but what we can do is a static balance which involves finding out which pole is the heaviest and reducing its weight by drilling bits out of it until it is equal to the others, It may be necessary to remove weight from 2 pole in order to obtain a god balance.
The easiest way to do this is to set 2 level razor blades in some modelling clay and let the armature roll down the edges it will come to rest with the heavy side down. Using a small dill bit remove metal from the pole face and repeat the process until all three poles weigh the same and the armature does not rest in any one position when allowed to roll down the blades. If done properly you will get a much smoother and higher revving motor, but if you are unsure of this part then leave it out and run the arm unbalanced you will still end up with a quicker motor.



Step 6

Magnets and motor limitations

I wont harp on about magnets much in this article only to say that in any electric motor the main limiting factor for performance are the magnets, you can have the best armature in the world but if the magnets are poor the motor will just overheat and die .You will also have poor brakes and acceleration
Chose your wind to suit the magnets I have made a list at the end of suitable winds for the motor in this article and for the scx motor
The scx magnets are better than the Johnson but in both cases I would get some very thin steel shin and place it behind the magnets to reduce the air gap This will improve the magnetic field and increase the torque, but it will reduce the rpm but the motor will respond better and run cooler.
The other limiting factor is the brush gear, the end bells of the Johnson and scx are made have quite easily melt able plastic so if you wind with too thick a wire you will melt the brush gear due to the heat generated.
The scx motor has probably the worst comm. I have ever seen but the rest of the motor is good so when I wind these I usually take a com off an old slot it /parma or Johnson and replace it before I start.

Step 7

Rebuilding the motor
We are now ready to reassemble the motor this is basically a reversal of the disassembly, make sure the armature spins free in the can with about 5thou end float no more especially if you have shimmed the magnets.
To get the best out of your motor you may find it necessary to increase or decrease the brush pressure, Run the motor for ½ an hour on 3volts to bed the brushes in and generally check every thing is ok using a light lubricant on the bearings Then you can experiment with the brush pressure, increasing it slightly by bending the springs will usually yield a bit more rpm

Step 8
Installation
You may be shocked when you put the motor into your once docile car I have had tyres flung off the rims so glue and true every thing
Also you will probably need to up the gear ratio A good start would be a slot it 8 tooth pinion but it depends on car and track

Results
The motor used was dyno checked before at 26300rpm
After the rewind it gave 36300rpm an increase of 10,000 RPM

Usable winds

Johnson/Mabuchi 111/13uo standard mags

120-140 turns 38 SWG 5 degree advance, home use
100-120 turns 36 SWG 5 -10 degree advance club /scalex use
70-80 turns 34 SWG 5-10 degree advance, club, scratch build use

SCX standard com
120-140 turns 38 SWG 5 degree advance

SCX with better com
100-120 turns 36 SWG 5 -10 degree advance, club /scalex use
70-80 turns 34 SWG 5-10 degree advance, club, scratch build use

These winds all have worked for me over the past 40 yrs on various motors
Rewinding is not such a black art give it a try

Sorry about the photos but my camera is giving focus problems I think it needs a rewind
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I cant wait for monday.. should be a reet laugh!
I can shoot a video.. just getting it online..
I need to know how to get avi files onlineyou ya to watch

Rob.
3
What did I mean by popping a cap in someone's ass? Well, that's actually slang for shooting someone i.e cap=bullet.

However, cap is used quite a lot to mean capacitor. If a capacitor is fed too much it explodes ("pops") with bits of silver paper everywhere.

If Inte's car had a full driver in it then by a small stretch of the imagination a cap would explode under the driver's ass


There ya go!!

Inte...careful now y'hear?
make sure the camera is rolling!

Mark
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Difflock, according to my friend Camp David, it means something else entirely.
A question for Grah: in our club some friends rewind their slot-it 29000k with good results and they use 18G wire, also without balancing the armature; I want to know how many turns are needed and how the number of turns will improve power, speed and brake power.

Thanks
Ciao
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Sprint if they are using 18g wire I wouldnt like to stand to close to it!It will melt the endbell and insulation within seconds. The fastest wing cars only use 23g american which is the equivalent of 26 uk swg approx I would not go thicker than 36 uk swg on this motor as the brush gear isnt up to it 100 turns on each pole .
hope this helps
2
Grah, we used to joke around here about arms wound with one turn of coat-hanger wire...
never seen any arm wound with something heavier than 22G (short-lived ballistic missile it was!)
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This reminds me of when I was about eleven years old and at my most inquisitive.
I was most fascinated by magnetism and electricity.
I found a library book on how to carrry out a few home experiments.
I seem to recall the first one was making an electro magnet by wrapping a few turns of insulated wire round an old steel Meccano screwdriver and plugging it into the transformer of my Rovex/Triang train set. The wire was about a foot long section of multi-strand insulated stuff that was commonly used to connect the transformer/controller to the train track.

This crude electro-magnet's power impressed me enough that I next decided to try making an electric motor using a carved wine bottle cork as the commutator. I seem to recall the armature shaft was a Meccano axle mounted on a frame bodged together from more Meccano bits and pieces. Memory completely fails as to how the commutator was constructed but, again, the wire used for the windings was that thick multi-strand stuff from my model railway connections. The motor must have had all of 12-15 turns per pole. When I plugged it in to the 12 volt transformer, the useless thing would barely turn at all. So I calculated I could get about twenty times the power by jamming the feed wires directly into the mains supply! It actually worked for a good ten seconds, in fact right up until I eventually realised that the room had completely filled with choking smoke from the burning insulation and bakelite from the mains supply plug! I frantically wrenched the wires out of the plug holes where they had been jammed in with short stumps of pencil. It was probably the effects of the toxic fumes that have erased all further memory of this lunatic experiment from my mind, but it would appear that I did not actually succeed in setting the house ablaze and I think managed to completely escape being detected as the cause of some quite expensive rewiring during the following week.
Ah, those were the days!
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Tropi I told you not to tell anyone about that experiment of mine.. oh you did it aswell.. ok I'll leave now..
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QUOTE it would appear that I did not actually succeed in setting the house ablaze and I think managed to completely escape being detected

So, if I understand correctly, this shouldn't be a routine source of pride at my age now?


Good one, Tropi!


Inte... wait!... don't go near the mains with those caps!


As for the aforementioned 22G wind, it dates back to 1971 or so when us crazy 1/24 guys were running cut out 16Ds with single 24s, 25s, and double 26/27 or 27/28 arms. All but one of us had given up any hope of winding arms that could run with one from Steube or Mura, etc. One guy had an unnatural talent though, and his winds were very close even though he could only static balance versus the "factory" dynamic balanced winds. In an effort to bring himself up that last step towards the big guys, he started playing with some very wild winds. Things like 23s, 25/26 doubles, etc. He had fun doing this and wasn't upset if they didn't work. All went up in smoke in rather short order. To great applause, of course!
But the best was his 22G attempt. The motor revved like crazy on the bench - howled like a banshee! So in a car it went, and out onto the 155 foot custom track with dual bus batteries for power. A few slow cruise laps, then he started pushing it - the thing had little torque but man, did it scream down the straight and through the banking - faster than anything we'd ever seen. I think it was probably 15 or 20 laps later (and definitely one too many), he was about 3/4 of the way down the straight when the thing literally grenaded. A huge plume of smoke was followed a split second later by shrapnel all over the track. (Picture a really big 1:1 engine failure but the car stops dead because the drive train is locked solid). The endbell had melted, despite heat sinks, and the comm had exploded, firing its own bits and many of the endbell parts out the back of the car. What was left was a smoking hulk in the banking, with debris everywhere. The smoke and smell blanketed the entire raceway. When it finally cooled, we checked the thing out. Above the motor, the lexan body had warped and blistered from the heat and the paint was burnt. Some of the chassis solder joints around the motor had obviously liquified and shifted. The plastic Cox spur gear had been melted by the pinion after the car stopped. The armature windings were charred, thrown from the stack, and jammed between the stack and magnets. It was total and complete destruction. Someone later calculated that the thing was probably pulling 20 amps! ...for a brief period....


...sorry for the long story... but it was absolutely the most memorable slot car blow-up I've ever experienced. Wow, maybe food for a new thread!
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I think I have made a mistake on the wire diameter used here
; tonight I will ask the friends and check their motors.
Ciao
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Thank you Fergy for that inspiring anecdote. I am going to rewind a johnson 111 with 22 gauge immediately and run it round and round a banked circle until I am able to recreate that scenario in all it's sensuous glory. I can smell it now!
7
yeeesssssss.......... i shall have to get some wire to put on that std scaley that i hacked apart and did nothing with........then i need saftey goggles& a bulletproof jacket!!!! this sounds like fun. now shall i put it in my brothers lola and watch him blow it to pices revving it
ill probbably get grounded for years!!!!
not such a good idea. i shall try this though. what do ya think will happen if i stick some wire of an old washing machine armature in it? or i have an electric scooter armature i think.......
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TO THE SHED!!!!!! *runs away cackling madly in the direction of shed*
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